What a weekend. Worked on the tune a little bit more Friday night and got it cleaned up and loaded the manual speedo segment swap with no luck. Got a ton of stuff done on the car though that night.
Got up 4 am on Saturday ( I have terrible insomnia lately so 3 or 4 hours of sleep is kind of normal for me) and got to it hoping to make it to cars and coffee. Had a bunch of stuff to get done. Pulled the drivers side wheel and tire off and fixed a little damage from tire hitting and pulled that fender out another half inch for clearance, much better.
Got the old front bumper trim cleaned and presentable, pulled the bumper again, installed old trim, rehung bumper and got it aligned. Pulled passenger door panel and installed lock cylinder, freed up all lock cylinders and got the door locks working. Installed the drivers rear window finally.
Hard wired in the ground wire for the AEM to Serial port adapter so I can simply plug in the cable in the glovebox to data log.
Got the car up in the air and did a nut and bolt on anything critical, found a few things loose, so got them snugged up, torqued suspension hardware and got the car on the grounds, quick torque of all the wheels and we were ready for cars and coffee about 7:45.
I got about 500 feet from the house and the car started to stumble and run horribly. Backfire the whole works. Something going on, get back to the house and start looking around. Luckily Micheal was around so he remoted in. Bank 2 misfire, no o2 operation. So I start digging in, could be plug wire and also he recommends only running Denso or Delphi 02 sensors so I run some errands, get some new plug wires, new OEM o2 sensors but in my gut didnt think that was the problem.
Install parts, no fix, so I get it running and start pulling bank 2 plug wires and no change, I had no bank 2 firing. Start looking at grounds and sure as **** find that the ground wire for bank 2 coil packs on the back of the head never got tightened down and me doing some clean up back there caused the connection to get lost.
Back to square and the car running again but I burned up all day Saturday. Picked up some parts from the twins and had a nice dinner.
Got up Sunday and got back in the garage, installed new swing out tire carrier on the JK and fullsize spare tire finally.
Tuner DM's me at 9 and says you ready to tune? I say hell yes.
So we go do some driving around, some logs, some tuning and he has me run the car into boost, and a little more and a little more.
This thing is a riot, instant power and wheel spin. He did everything remotely and did an amazing job. We have everything setup, fans, tune, tip in, driveability.
I drove it around a bunch yesterday, have a few little things to iron out, rearend howls like a coyote so that is next to address. Clutch is a little chattery but hoping that gets better with a little use.
First fuel stop
LSX badge installed
For all the haters of the carpet color, I have to say that spending some time in this space has been nice, the interior came together pretty damn well.
Now the bad news. The rearend is trash. Needs a full rebuild. SO True Track is on order and will be here in a couple of days will have gear guy Dan go through rearend and replace as needed. Limited Slip is super chattery and the dreaded howl.
It desperately needs more muffler, the car is annoyingly loud. Ill order up a U bend and a muffler and get going on that in the coming weeks.
VSS Still doesnt work, going to hard wire to the RacePak dash assembly, also need to add a trigger to dim the cluster.
High Beams dont work at all, so gotta figure that out.
Pretty minor stuff in my opinion.
Burnouts to come very, very soon.
Sean